Saturday 17 March 2012

War against turd

Not a lot has been happening on the mod front lately, more so I have been spending some time and effort on the mechanical / maintenance side of things. Having to replace the blown welsh plugs brought to my attention the fact that the car might need some mechanical TLC, so as a matter of course, I recently installed a full regrind kit, new thermostat, coolant / radiator flush, got rid of the emissions crap on the carburettor, installed a fresh electronic distributor, and gave it a nice clean down with some degreaser. The car runs like a dream, and I can rest assured it won't likely experience any more hiccups.

I have spent the weekend attacking the doors with some VHT vinyl dye (satin black, not taxi-spec gloss), relocating the head unit, fibreglassing the dash / facia, and installing a 12" subwoofer and amplifier. The car looks and goes well now. Time to finish the interior now with fresh black carpet, VHT-dye the brown seats a light tan colour, recarpet the parcel shelf, and finally move on to the bodywork. After this the project will more or less be complete :)

Sunday 22 January 2012

Leaky Bastard!

Last week driving home I ended up stranded, though luckily one street down from my house. Initially I thought the worst - head gasket - as a mountain of steam poured out the back of my car and the temperature gauge rose. Being the preventative, pedantic driver I am, having had bad past experiences with my Soarer and Bluebird, the latter car rendered ruined due to overheating, and a warped head + block, I switched the car off immediately, and babied it home with a mate and a tow rope.

The initial diagnosis proved wrong - the head is still perfectly sealed, and I was dumbfounded as to why there was in fact steam coming out of the engine bay rather than being combusted, not to mention the car was not holding water whatsoever, even whilst switched off. I then discovered water leaking onto the starter motor, and dripping down directly onto the exhaust. Using a mirror, I found the cause of my problems - a leaky and badly corroded welsh plug.


The 35mm piece of metal which left me stranded.

Not content with the prospect of paying a silly amount of labor to have a $3 part replaced, I went and bought 3x35mm plugs, and 3x45mm plugs, and some loctite sealant, and removed the carburettor, and manifolds (all on the passenger side). Most of the time when a welsh plug goes, it is an engine-out job, but the beaty of the '55 is the 4K is so damn small, ample room is left for bashing out the old plugs, and replacing them. A few hours, and a lot of swearing and cursing saw the carb and manifolds off, plugs replaced, and car up and running once more.

Next stop, VHT dye the interior matte black, a custom stickerbombed dash facia (tastefully I assure you), LED cluster conversion, and maybe then I'll consider prepping my beast for sale. I have another project in mind in the very near future - the words Lexus, GS300, and VIP are relevant here.